head gasket gone

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daewoomofo
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Post by daewoomofo »

damn!
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yeah i cant type, so what big freaking deal!
exist3nce
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Post by exist3nce »

Wow so soon..... thats no good. Let us know what you find.

C20LET/F28 swap? haha
2004 Optra/Forenza/Lacetti - 225whp - Haltech Sprint500 - CT12B - Getrag F28 6spd - KW V3 Coilovers - FX35 Retrofit
2002 IS300 5MT - 615whp - AEM EMS - GT4088R - Built 9.5CR - R154 - TRD LSD - SupraTT T/B - Varex - LS430 Retrofit
Efratech
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Post by Efratech »

Pir0 wrote:Maybe the heads gone pourous... was it a Coscast head? Or a GM one?

Could be potentially disasterous :S
you get oil in the water when they go pourous... its a GM

exist3nce: i want but cant!!!! :cry:
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
Efratech
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Post by Efratech »

once again, the headgasket is gone... :evil:

deffo need headstuds.
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
Pir0
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Post by Pir0 »

You reused the old ones?! ><
SAZ
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Efratech
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Post by Efratech »

update... about a month ago

i took the car apart about a while ago and for some reason one of the water galleries in the head was corroed enough to be near the cylinder 4 chamber.. and its where exactly were the headgasket was blowing. so i think i found the source for the problem.

So took the head to a repair shop... some welding and a skim... almost like new. i put the engine together again and a mate helped me to torque the head (im not used to do that) so yes is up and running again.

now... the differential has some play its seems and its generating a big vibration to the hole car... need to look for another box
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
Efratech
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Post by Efratech »

headgasket gone again on saturday night....

a missfire started on cylinder 1... and white smoke... took the spark plug out... water...

i took the cam cover out last night and only the cookies where missing... chocolate.

i checked the headbolts and they're very tight.

i dont know what it is now.
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
gse_turbo
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Post by gse_turbo »

...that sucks, I still have the head studs and gasket you ordered here if you want them.
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Efratech
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Post by Efratech »

yeah i know you have them, budget is tight now, well always :). PM with the final price. (email full of spam, so im not checking it)
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
MMamdouh
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Post by MMamdouh »

too sad to here that bro

what can cause that?
was it the same area that developed problems on the first gasket?

MMamdouh
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Pir0
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Post by Pir0 »

Warped or cracked head?
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Efratech
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Post by Efratech »

yesterday i went again at the bolts and they did tight again a bit... but after we did it it was still letting some water in.

So... will be off again. once its all back together i wont past 4rpms so it wont blow out again.
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
Efratech
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Post by Efratech »

i changed the gasket again, yesterday... but changed the brand of the gasket, this one seems better quality (not original ones around at the moment) and the car seems to like it better.
'88 Pontiac Lemans GTE - 2.0 16v XE - fully programable ECU, Custom made intake manifold and other bits.
146.6WHP/135lb.ft - 14.81@94mph
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